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bandmmorris

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Posts posted by bandmmorris

  1. The motorhome MSRP was around $330,000 new and included over $30,000 of options. This motorhome has a 400HP 400ISL Cummins diesel engine (No DEF) with side radiator, Roadmaster raised rail chassis with tag axle, 10KW Onan diesel generator, Aladdin System, power patio and door awnings, slide-out room toppers, Aqua-Hot water heater, macerator black / gray water pump, washer dryer combo, 2 leather recliner chairs and foot rests with heat and massage, sofa that converts to queen size bed, 3 burner range, double sink, convection/microwave oven, roof top satellite dish, 50 Amp power cord reel, power water hose reel, pass-thru storage, 1 full length slide-out cargo tray, keyless entry, bay heater, 10K lb. hitch, automatic air leveling system, color 3 camera monitoring system (rear and sides), Magnum inverter, ceramic tile floors, all hardwood cabinets, solid surface counters, king sized bed, 3 ducted roof A/Cs with heat pumps and 2 Smart TVs.

    I am the 2nd Owner. Coach is in great condition with some minor body flaws and everything works as it should. It has 66,578 miles with new engine and turbocharger approximately 1500 miles ago by Cummins Services (nearly $40k). The motorhome has upgraded and larger TVs, upgraded sound system, residential refrigerator (approx 1.5 years ago), new front AC (approx. 1.5 years ago), LED inside lighting, 600 watts of solar panels, new mattress and topper, new batteries 1.5 years ago, Aqua-hot serviced approximately 3 months ago. Only thing needed is 2 front tires should be replaced due to age. Selling is because we are downsizing.

    Additional photos available by emailing bandmmorris@yahoo.com. Scammers don't waste my time.

    Bathroom 3.JPG

    Bedroom 3.JPG

    Bedroom 6.JPG

    Bins 1.JPG

    Dash 5.JPG

    Exterior 1.JPG

    Exterior 3.JPG

    Exterior 7.JPG

    Exterior 18.JPG

    Interior 2.JPG

    Interior 3.JPG

    Interior 6.JPG

  2. I took both of mine out and after buying replacement televisions and figuring out how I wanted to mount them I took some paneling and cut out pieces to fill the gap between the cabinet and television. I stained them to match the existing wood and put a few coats of varnish on them before installing. They came out really well.

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  3. I had this problem a few years ago. It turned out that inside the cord reel there are 3 contactors, 1 for each hot leg and one for the ground. One of the hot legs had become corroded / burned and would not make contact thusly only one hot let. At first I could rotate the reel slightly and get contact. Ultimately that would not work. I took our the reel and make a new contact out of a piece of flat copper I bought at a hardware store. Once replace everything worked fine and still is working fine. It wasn't a big effort to remove the reel (through a panel in the closet) and replace the bad contactor.

  4. Since I have lithium batteries and solar panels it will work for boondocking for a time. Without these it still works for boondocking, but may have to start generator periodically to charge batteries. Frig does not pull much power, particularly if not too hot outside. I have the original inverter/charger. 

  5. The one you have appears to have screw on connections while the ones I have use quick disconnect style connections. You could use one of these, but would have to purchase the quick connect adapters to be able to connect to your hoses. Also, the ones I have are 2.9 gpm (Flojet model 03526144) and 5.7 gpm (Shurflo model 5900-0201). Let me know if you are still interested and I will get the shipping cost which will likely be less than $20.

  6. Thanks. How well did the insulation work. It appears much thinner than what I have which is around 1/2 inches thick. 

    On 3/22/2023 at 8:37 PM, LakeBob said:

    I recently rebuilt both the engine covers on my Dynasty.  The hard part is cleaning the surface to get good adhesion. 

     

     

    What insulation did you use.

  7. I seem to have lots of boost (up to 37) and power seems good. I have no codes. When I replaced the turbo the replacement turbo came with a new actuator. I found the issues as a result of decreasing boost and performance and an increase in black smoke during my last trip. I don't think I have any more boost leaks as the system was checked throughly during the repairs, but I will try to check again. 

  8. I just replaced a cracked turbo and repaired air leaks in the intercooler and one of the hoses on a 2007 Monaco Camelot with a Cummins ISL400. After all these repairs (done at the same time) I now find that my fuel economy decreased by about 30% from when I had all these problems. I spoke with Cummins and they were no help. Any suggestions on problems to look for would be appreciated. By the way, the fuel filters and air filters were replaced.

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