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engine103

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  1. Paul, that may be true. Draining the holding tanks revealed no moisture or oily substance so I think I'm good there. But, your right, I'm not going anywhere for a while and plans are to replace it. Thanks, Jim

    On 10/13/2023 at 1:23 PM, Jdw12345 said:

    I would check the air governor for proper operation.

    I would replace the purge valve next, jmo.

     This might help.

    https://www.wabco-customercentre.com/catalog/docs/mm34_web.pdf

    jdw12345, thanks for the link, going into my file! Jim

  2. Have noticed lately that my air dryer is not purging as it has in the past. I have listened for it as the compressor reaches operating pressure, nothing.  Also have used an aux compressor to fill the system to 120 PSI, still nothing. Yes, the filters have not been changed in maybe three years. Could the pop-off valve be stuck? Could the filters be so clogged that it can cause it not to release?

    Jim Eastburn

    2000 Signature

     

  3. I have a Goo Loo GP 4000, which saved me from a tow. Due to an alternator failure, we lost the chassis battery and were unable to even get a click out of the starter. Called a tow company and they said "try one of those battery jump-start things if you have one." Well, I had just purchased one a month before and was lucky enough to have it with me. Hooked it up to the starting batteries hit the boost button and it spun that ISM 500 like I had new batteries! I now own three and will not travel without one.

  4. Bill, this might be a fix or not. My steps would not come out. The step light was on when I opened the door, so I know I had power there just no action. There is a four lead connector by the motor. When I unplugged it the step light went out. When I reconnected it, the step opened, scared me! I opened and closed the door several times just to make sure it wasn't messing with me. I opened the connection again and applied some Dialectric grease in it for a better connection. Worth a try. Jim

  5. Thanks Ivan and Frank. Sorry for thee upside down pictures but... Ivan there is what appears to be a ground wire from the bottom battery connector over to the side of the case that you don't have. Should I leave that where it is? This is the original alternator to be rebuilt and the box shows what they replaced it with. Thanks, as usual for all the help. Jim

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  6. No, that is not the original alternator, that is one they sourced for me. My original is sitting on my bench waiting to go to the shop for rebuild. I had better than 1/2 fuel on board so that was not the problem with the generator shutting down. Basically after the generator quit, I ran until the batteries were exhausted. The jump start pack I used is a Gooloo GT 4000. It gave ne enough juice to start and could go a few miles with just keeping it connected to the batteries. 

  7. Engine Electrical Problem

    Traveling through South Dakota last week, I began having problems with keeping my generator running while traveling. Soon after this I lost cruise control then noticed that my voltmeter had dropped to zero. Within a few minutes the transmission dropped down to 4th and what I believe went into limp mode which resulted in a top speed of 55MPH. Hoping to press on to Sioux City another 30 /40 mile where we could get some help and avoid a tow.

     As we pulled off the interstate it was obvious that we were about to lose all engine power but were able to make it to the truck parking area where it just died. Across the street was a large truck repair (First State Truck Repair) but we are dead with no starting power. Of course, this was a Sunday, and they were not open. Monday, I called a tow company, but he was relucent to come out for a ¼ mile tow and suggested if I had a jump start box it should get me started and if left connected would get me across the street to the shop, and it did.

    “I” told the shop that it was an alternator problem and so they replaced the stock alternator (Cummins ISM 500), with a new alternator but had a problem getting a charge to the batteries and said there may be a problem with the battery isolator, they could replace it or wire around to make it work which I had them do so I could get back on the road.

    Now I would like to undo what they did with a new isolator and my rebuilt original alternator. But I need a picture of how the high voltage was connected at the isolator.

    Ivan, would you mind posting a picture of the High voltage box to use as a guide? Thanks, Jim

     

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