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Paul Busch

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Posts posted by Paul Busch

  1. I don’t know if my 05 sig castle is the same but I have been having trouble with the low beam staying on. My high beam switches on and off with column lever but low beam light go out and will not come back on. There are wires coming to smart wheel controller in side electrical bay and one of them was scorched. They are labeled high and low beams. I replace smart wheel controller, light switch and still had trouble. Turns out wiggling wiring harness from panel going through to front of coach was a loose connection. Cleaned all grounds and connection worked for me.

    paul

  2. My 2005 sig castle has an oblong mirror detail in the living room and smalller one in the bedroom. One has 3 bolts and 2 for the other. They are under the trim detail and easily reached with a socket extension. The other side is hinged so have someone help hold it. Easy to do with help.

    paulb

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  3. Maybe someone could help with this. I have only used 50amp shore power in my 05 sig. I moved today and have to use 30 amp for a week. None of my 110 outlets work when I plug in to the 30 amp panel. When I unplug shore power everything works as should.
    I have only owned coach 5 years so this is new to me.

    paulb

  4. I just tapped all three of my units and one used stop leak with a charge of R22, send one was full and third one need a top off.  Been working great for 4 months. The taps are 4.50each on Amazon. The stop leak works great. I paid 90 for a tech to climb  the roof and check and charge what was needed.

    05 sig

    • Thanks 1
  5. George. 
    I was coming through West Virginia last October it started when I was climbing the long hills and quit descending and after a few hours the check engine stayed on. I might have had the tranny in Economy mode. I couldn’t tell with the light and sunlight. The tranny was stuttering while up shifting but that cleared up ounce we got out of the hills. According to Aladdin engine and tranny never overheated. The red flashing light is on all the time now when running. I can lower the warning noise and put tape over the red light to get by. It never has smoked and doesn’t now.

    I had a mobile tech come out from San Antonio Monday to read the codes. He seemed competent. He said the was an old code FLUID LEVEL SENSOR which someone on this site had suggested. I had changed that last week. He cleared that old code and it stayed cleared. My coolant is full. My oil is clean, no coolant in it. My tranny is full. It was about 3quarts low which I added a couple weeks ago. I changed tranny fluid and filters a couple years ago, about 15,000 ago.

    I know cleaners might not resurrect a failed injector but am hopeful I might be able to clean it if not to far gone since no smoke. One of the problems I have with these guys is for 165.00 they stand around, scratch their heads and say they don’t know. The accumulated knowledge on the site is the best resource I have come across.

    I changed fuel filters, hydraulic filter and fluids all are good. I have not really added any additives so am going to give it a try. 
    thanks Paul

     

  6. George,

    I am leaving in a little while and won’t be able to order the optiLube you recommended. I picked up some BG 245 from NAPA. Do you think it would hurt to run it for a tankful till I get to where I will be for a while to order the other product?

    I also have some DieselKleene with Cetene Boost. Could I run that? I am trying to clean up one injector before it dies. I am leaving on the 16th for about an 750 mile trip and will be parked for another month then.

    paul

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